Page 2 of 2

Re: 6.OH

Posted: Tue Feb 12, 2019 11:41 am
by blackford
Some of the local crew have heard, but I bought another 6.0 motor to drop in with 74k miles on it. I'm having a shop put it in and they'll transfer over the studs and the bulletproof egr so I'll hopefully have this motor go for a while this time. I think I'll have it back on the road next week which is good news.

Re: 6.OH

Posted: Fri Feb 22, 2019 10:28 am
by BadAssEddie
Nice

Re: 6.OH

Posted: Sun Mar 24, 2019 8:57 pm
by blackford
A few weeks ago the truck got back on the road. Refurbished turbo, arp headstuds, bulletproof egr cooler, and coolant filter. Since then I've started building a front bumper. After I finish this I'll work on steps and a rear bumper.

Re: 6.OH

Posted: Wed Mar 27, 2019 9:57 am
by Mr.WJ
Not sure why, but the picture was flipped. Fixed it for you.

Re: 6.OH

Posted: Wed Mar 27, 2019 6:18 pm
by blackford
Thanks, I couldn't figure out how to fix that

Re: 6.OH

Posted: Thu Apr 11, 2019 7:59 pm
by blackford
After bashing the truck when I took it to the shop I found a new hood and a few other things. Kept working on the bumper so its almost done at this point. Just needs to be sanded and painted. Its come a long way since looking like I had teeth coming off the grille.

Started the tear down on the old motor and haven't found anything too suspect yet. Plenty of metal in there but the source is still to be found. I've yet to tear open the hpop, but my buddy is putting his money on a rod bearing. Thankfully the cylinders look fine with the heads so I can salvage those at the very least.

Re: 6.OH

Posted: Fri Apr 12, 2019 1:27 pm
by YellowDodgeBrian
So compound turbo the bullet proof one?

Re: 6.OH

Posted: Mon Apr 15, 2019 2:24 pm
by blackford
As much fun as that might be.. I think I'll stick to doing that to a project vehicle instead of my daily

These were the problem children. Got two of them out and the third is still stuck in the block. At the end of things there were three different cylinders that had an intake/exhaust lifter gone bad